Some knew that I had decided to swap an L26 into the 95 Transport.. It was a bit of a Pain, but what swap is without pain in some manner when going from a series I 3800 to a series III bottom end..
Towards the end of the 3800 Series I Tuned Port Injection useful life I was running 20-50 to keep the oil pressure up and to mask the light knock that was present at hot idle.. I knew this engine would be short lived as it was getting tired.. I did have my fun with it... The ported parts and the 1.8 rockers do make a difference in the Tuned Port 3800 L27.. All worth it in my eyes.. I just wish the engine would have held up and stuck with me for another 100,000 miles.. It was a torquer from the word go..
So the next step was to locate a motor to replace the L27 with... All of them were high mileage and expensive for what I was willing to spend on an L27 3800... In our research we found the L26 motors to be in good supply and cheap.. We ended up with an L26 from the LKQ( not a U pull it LKQ )... The engine had 41,000 miles on it.. Price was $250
S we picked up the motor and got it back to Sandrocks house so that he could do soem wiring for me..
we pulled the upper and lower intake off only to find this to be a very clean motor..


After I got the engine back to the house I yanked the oil pan to make sure it was clean and to reseal.. Gave me a chance to get a looksy at the bottom end components... Low and behold, sure enough they are Powered Metal rods..


After cleaning out the oil pan I ran a bead of Grey RTV and sealed the pan to the block..

There was one big problem here.. I later found out that the Front motor mount bracket would not fit with the aluminum pan in place... I had to remove the oil pan and install the Series II stamped steel pan to get the front mount bracket to be able to fit.. The good part is that the 95 L27 used the series II oil pan.. So going from the series III aluminum pan to the series II stamped steel was not an issue for the mount..
Not sure if it will be visible in the Pic but I did some minor port entrance kissing to smooth or round off the edge of the port so that the air flow will not have a step for the air to slow down flow..

Next it was time to do some porting on the lower intake...Compare the 2 ports on the left with the one on the right..


Along the way I had the gaskets for the front timing cover and the oil pan was off.. So I ended up with a Comp Cam for NA applications... Its a performance cam that uses the stock stall, and is good with Intake Mods..
Operating range is 1000-5500.. Stock Cam on the right

Timing cover after removal.. Happy to see it that clean..

Not a great Picture, but here is the Lower intake bolted to the heads.. Notice there is no step between the head and the intake..

Installed LS6 Valve Springs and Comp cam retainers.. I used the stock rocker bolts for the time I was installing the springs.. There were replaced with reusable rocker arm bolts..


At this point it was time to yank the old engine and clean up the subframe..


Managed to get the engine set in place on the subframe.. Installed the PS pump, alternator, compressor.. Oil filter adapter( could not use the U body adapter due to the location of the PS Pump )... Installed the new Rack and pinion as well.. New water pump..


Delphi series Alternator..

Had to use the 97 Power steering line from a Pontiac Grand Prix... Beat the heat shield up to make it work on the rear mani..

I had to notch this ear off the block to make the block to trans bracket work... Bolt hole locations were identical to the series I block... Difference was the ear that was there... Also had to cut 1/4 " off the top bracket to tail shaft housing to make it work..


Where the oil filter actually sits in relation to the frame and balancer



Next I had to splice and run new fuel lines as the stock lines would not work with the new engine / fuel rail.. I bought a fuel line repair kit a while back as i knew I would need it for this swap.. It has come in handy several times and paid for its self.. LOL
The Splices


The Motor ready to go in complete with wiring harness

A Big Thanks to Sandrock for doing the wiring for me.. Couldn't have done it without you boss..
Motor in... I removed the upper intake and EGR for easier install..


Most of everything installed..

2nd start.. It was a bit pissy as it was running off the L27 tune..

After this video the VATS in the L36 95 chip was walked around to allow the L26 to start and run off the L36 Bin File.. Once we got the L36 bin file to run the van we noticed we still had the stall issue... Turned out I had some not so good injectors... I removed the Rochester injectors and installed a known good set of Bosch L36 injectors... So far the idle is good( Has a little lope to it )... Starts and idles.. Drives pretty decent..
Also as I was going to the cam I decided to dump the 2.97 gear ratio I was running in favor of a 3.33 ratio.. While I had the drivetrain out I yanked the side pan and valve body and changed the drive and driven to 35/35 to make it an overall 3.33 ratio..
As of current... The van still needs an alignment... I need to get it to an exhaust shop to have the 95-96 Bonneville Down pipe attached, and run 2.50 Pipe to the muffy... Also the windshield has a nasty crack now.. I need to get with the insurance on that...
Been a very long road with this van.. But still moving along.. Once all of that is dealt with i will pull the interior... Do some sound deadening, clean the carpet and redo the head liner.. Moving along slowly...lol


















